With the main engine raw water intakes installed, I was ready to install the strainers, valves, and hoses.

This day has been a long time coming
I’ve mentioned many times before that the only areas inside the hull where we found substantial corrosion were pits in the aluminum near copper fuel and waterlines or bronze bolts and valves. The entire hull is now epoxy barrier coated, but I made the decision to also de-copper the boat to the extent possible.
So for the main propulsion engines, instead of bronze seacocks, I went with 2″ Forespar Marelon. Instead of bronze hose barbs and elbows, I went with 304 stainless.

Starboard seacocks installed without difficulty
Forespar recommends teflon tape or paste thread sealant for all of their Marelon valves and fittings, which use National Pipe Straight threads instead of Tapered. I used generous dollops of Gasoila JC-30 High-Fill to coat all of the threads that didn’t get epoxy barrier coated.

The port side was less cooperative

Can’t rotate the seacock because the handle hits the frame
Fortunately, the handle comes off easily.

Port seacocks are installed
The seacock inboard of the Marelon one is original to the boat. It fed raw water to the original Kohler genset. It’s in fine condition, and I barrier coated the body along with the hull after I had the interior hull sandblasted to keep green copper oxide from sloughing off. The only problem with it was the outlet was a 1-1/4″ hose barb. That became a bigger problem when I tried to remove the barb with a pipe wrench and it twisted off, leaving the threaded portion in the strainer body.

So I bought a really big drill bit

Then I threaded the hole with a 1″ NPT tap

1″ nylon hose barb will do the trick

I had a tube of Anchor sealant handy, so I used that on the gasket sealing surfaces

Same sealant for the strainer base


The air conditioner raw water strainer is installed with new gaskets and sight glass
Next I installed the main engine strainers.

To ease future maintenance, I put TefGel on the stainless strainer mouting screws
The main engine strainers are 2″ Buck Algonquin 70RWS200 in stainless steel. I bought these back in 2016. They’ve been sitting on a shelf in their boxes until just now.

Gasoila on the clean-out port threads will also help with future maintenance

The strainer drain port points directly facing the engine stringer, which isn’t optimal
Access to the bolt for the drain will be much better if I rotate the plastic sight glass a bit.

The threads were dry…I used TefGel when I put it back together

Reoriented sight glass is back in place

Hose barbs and elbows are fitted and pointing in the right directions

I made strainer mounts from aluminum plate left over from the aft deck enclosure build
As with everywhere else, the aluminum strainer mounts are coated with Bar Rust 235 epoxy.

Perfect!

Ready for the test fit

Nice!
I removed the strainer and started installing the hoses when I found a small problem.

See the slice in the brand new hose?
I just bought this hose at West Marine. Somebody carelessly cut the hose with a razor right in the middle of the length I bought. Fortunately, there was 6″ of this 48″ hose that I won’t need, and I was able to cut the four lengths I need and toss the damaged section.

It was extremely difficult to put the hoses on these stainless hose barbs
Pushing 2″ wire-reinforced hose onto barbs measuring 2-1/8″ across was a real bear, but I finally got them installed. Hose clamps will be mere decorations.

Boom…starboard side is done

Repeat the process on the port side

Uh…Houston…

…we have a…

…problem
All of the screws on both strainers were very tight, and there was no thread lubricant, so there was a POP sound when they broke free. But when I loosened these three cap screws, there was something off about the sound. On closer inspection, I saw that there were cracks in the acrylic near these screw holes.

These strainers were sitting in their original boxes since I bought them


It seems the problem was caused by no thread lubricant, the screws were torqued very tight, and the fact that the holes drilled in the plastic are slightly too small. The holes aren’t threaded, but the screws don’t pull out of the plastic once they clear the stainless they’re threaded into. I had to unscrew them all the way out. I suspect something akin to stainless galling (a kind of cold weld) happened. Twisting the screws broke the galling free and fractured the acrylic in the process.
I went online and discovered that not only is this model of strainer discontinued, Buck Algonquin no longer exists! It’s been bought out by some company I’ve never heard of (Hydrasearch), which has yet to respond to my inquiry asking if they have a solution for me.

Magical modern sealant to the rescue!(?)
I recently heard very good reviews of this Lexel sealant product, including some long-time users reporting that it stays stuck even after 5+ years of outdoor direct sun and weather exposure. So I’m trying it out in a bunch of different areas, and I figured I might as well try it out on this strainer. The sight glasses are obviously somewhat compromised, but I’m not keen on throwing out brand new, expensive strainers if I can MacGyver this manufacturing defect. A previous boat of mine had much more dire looking cracks in the sight glasses, but it never leaked a drop in the seven years we owned the boat.

Hopefully, a dab of Lexel will prevent the cracks from leaking or growing

Port strainer dry test fit

Hoses are installed!
I still have to install the hose clamps, but that’s a trivial detail compared to finally getting the last of the holes under the waterline buttoned up and the main engine raw water circuits basically done. If the boat had to splash tomorrow…it could! But first, I have to drill two new holes in the bottom.
BUT before I get into that, I want to clear up some space on my camera memory card by posting articles of things I got done over the last couple years but never got around to posting.
Next up in our 1969 Chris Craft Roamer 46 Refit: The V-berth Door































